Laboratory Investigation into the Performance of an In‐Sewer Vortex Flow Regulator
In: Water and environment journal, Band 7, Heft 2, S. 182-189
Abstract
AbstractAspects of the hydraulic performance of an in‐sewer vortex regulator have been studied. These devices are increasingly used in stormwater management schemes, but their characteristics under a variety of prototypical situations have not been widely disseminated. The study used a full‐size laboratory mockup of a section of sewer and associated manhole with facilities for measuring discharges of up to 60 1/s. The performance of a typical vortex flow regulator was investigated under both steady and unsteady flow conditions. The steady head‐discharge relationship revealed the expected 'kick back'region (during rising head); however, this was less pronounced during falling head. Under unsteady conditions, vortex initiation was affected and a hysteresis effect was noted. The influence of downstream surcharge was significant at lower upstream heads. Theoretical comparison showed that to obtain equivalent performance, an orifice of 62% of the diameter of the vortex regulator would be required, and 25% savings in storage could be made.
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